Sunday, January 27, 2013

On The Level

With the bottom planks off, we are ready to get the boat setup and level.  Using 2 floor jacks, first the rear, then the front dollies were jacked up and the sawhorses assembled.


Crawling under the covering boards, it was tight quarters to assemble the sawhorses.


Setup on the adjustable sawhorses, we removed the bottom plank battens and the topside chine planks.  Then we began to level the chines port to starboard, first at the sawhorses and then each frame.  Using a 6’ level with equal length spacer blocks, the wedges under the support of the sawhorse where adjusted.


Next, we added supports about the perimeter to support and adjust the twist in the framework.  Cinder blocks, 2-2”x6” blocks, foam rubber and wedges are setup to lift frame stations into level.


Finally, the line projecting laser level was used to bring each frame station level port to starboard.   The wedges between the 2”x6” blocks were adjusted to raise the low side at the major frame stations until each was level.


A final check to confirm the sawhorses were still supporting the bilge stringers and all stations were level, the wedges were super glued to prevent them from moving.


Now we can begin pulling the framework back into shape.

Saturday, January 26, 2013

Bottom Removal

With the boat on the dollies, we began removing the putty from the bottom for removal of the planks.


The putty was drilled out using a modified a 5/16” wood spade bit.  The bit removes the putty to the screw top and, most of the time, the small tip would find the slot of the slotted screws.


For the few screws forward, above the waterline, the factory installed wood bungs.  We used a scribe to split the bung and pop the bung free.  With all of the screws exposed it’s time for the screw gun.  Most of the screws came out easy, except for the few broken or striped ones.


At some point, a previous owner installed 5200 rubber in the gaps between planks in an attempt to slow leaking.  This is not a good idea on original planking because with each swelling cycle the plank no longer has room to move and pushes the chines out of the frame landings and can cause the planks to cup.  The planks came off easy after cutting the 5200 in the gaps and a little prying at the striped or broken screw locations.


Several hours later, we have a lot of brass screws to recycle.

Tuesday, January 22, 2013

Bottom Inspection


With the Resorter bottoms up, we were able to take a closer look at the bottom condition.  There are several cracked planks and some hairline fractures mid-width of the plank.  In addition to the joints leaking, these cracks and fractures also allowed water in.  For 61-year-old wood, it is pretty brittle and lifeless. 


There is also a repair area on the starboard garboard plank adjacent the strut and rudder shaft.  There is an oak-backing block with steel screws from both the top and bottom.


On the opposite side, there is a hard, gray filler material over the plank, keel and a portion of the adjacent plank.


Digging out the material revealed a deep, straight, athwartships gouge in the plank, and some broken pieces on the edge.  It looks like there was a prop blade strike, maybe a broken blade?


After removing the backing block, it was determined the plank is fractured.  It is not broken completely thru but is very weak without the backing block.

Tuesday, January 1, 2013

Rolling Over

Now that we are ready to roll the Resorter over, what are we waiting for?  On Christmas Day, with family able to help, we tried turning the boat over.  Unfortunately, the lift straps wanted to walk off the rollers.



So we set the boat back onto the cradle and tried several different ideas to solve the problem, but none worked.  Finally, we decided the rollers needed the shoulder machined off, so we sent them off with my dad for modification.  Lights out for now.


On the following Sunday, with a few more bodies to help with the roll, we tried again with the adjusted rollers.


Up went the chain hoists, out went the cradle and slowly we started turning the boat. 


And still, the straps tried to walk off the rollers.  But, this time with the extra help we simply lifted the boat, re-positioned the straps and continued on.  Checking for clearance with the garage floor as we neared vertical, a little higher with the hoists was all that was needed.


Pulling the port side under, and stopping a couple of times to adjust the straps, we finally had the boat upside down.


Holding the boat to prevent it from trying to right itself, we lowered it onto some dollies with high density foam padding, and started breaking down the lift rig.


Here is a time-lapse video showing the successful flip.


Thank you to everyone who helped build the flip rig and work thru getting the Resorter on her back.  Now it is time to get the bottom planks off to start frame repairs.